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dc.contributor.authorBennett, Gareth
dc.contributor.authorLiang, Yong
dc.contributor.authorZhao, Kun
dc.contributor.authorChen, Yingchun
dc.contributor.authorZhang, Longjun
dc.date.accessioned2019-10-01T13:51:22Z
dc.date.available2019-10-01T13:51:22Z
dc.date.issued2019
dc.date.submitted2019en
dc.identifier.citationLiang, Y., Zhao, K., Chen, Y., Zhang L. & Bennett, G.J. An Experimental Characterization on the Acoustic Performance of Forward/Rearward Retraction of a Nose Landing Gear, International Journal of Aerospace Engineering, 2019, Article ID 4135094, 2019en
dc.identifier.otherY
dc.identifier.urihttps://www.hindawi.com/journals/ijae/2019/4135094/
dc.identifier.urihttp://hdl.handle.net/2262/89593
dc.description.abstractThe modern undercarriage system of a large aircraft normally requires the landing gear to be retractable. The nose landing gear, installed in the front of the fuselage, is retracted either forward or rearward. In the forward/rearward retraction system, the landing gear is normally installed to the trailing/leading side of the bay. When the incoming flow passes the landing gear as well as the bay, the installation that corresponds to the forward/rearward retraction system has a significant impact on the coupling flow and the associated noise of the landing gear and the bay. In this paper, acoustic performance of the forward/rearward retraction of the nose landing gear was discussed based on experiment. The landing gear bay was simplified as a rectangular cavity, and tests were conducted in an aeroacoustics wind tunnel. The cavity oscillation was first analyzed with different incoming speeds. Then, the landing gear model was installed close to the trailing and the leading side of the cavity, respectively. It was observed that installation close to the leading side can help disturb the shear layer so as to suppress the oscillation, while the trailing one can make the landing gear itself produce lower noise. Accordingly, conclusions on the acoustic performance of the forward/rearward retraction of the nose landing gear are made.en
dc.language.isoenen
dc.relation.ispartofseriesInternational Journal of Aerospace Engineering;
dc.relation.ispartofseries2019;
dc.relation.ispartofseriesArticle ID 4135094;
dc.rightsYen
dc.subjectAircraften
dc.subjectAcoustic performanceen
dc.subjectNose landing gearen
dc.titleAn Experimental Characterization on the Acoustic Performance of Forward/Rearward Retraction of a Nose Landing Gearen
dc.typeJournal Articleen
dc.type.supercollectionscholarly_publicationsen
dc.type.supercollectionrefereed_publicationsen
dc.identifier.peoplefinderurlhttp://people.tcd.ie/bennettg
dc.identifier.rssinternalid204059
dc.rights.ecaccessrightsopenAccess
dc.identifier.rssurihttps://doi.org/10.1155/2019/4135094
dc.identifier.orcid_id0000-0002-1621-7533


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